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02-07-2014, 12:16 AM
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#1
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Banned
Join Date: Apr 2013
Location: Gainesville,Tx
Age: 39
Posts: 2,405
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You would be surprised what people will do to try and not be accountable. I knw that another business would do everything to try and tune a car so they could make money. So Tsm not wanting to even mess with it raises some flags. Let me ask you this....why was it not tuned right the first time? Why were those afrs lean? Why did they let it leave like that?
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02-07-2014, 12:23 AM
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#2
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Senior Member
Join Date: Jan 2014
Location: TX
Posts: 285
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Originally Posted by re-rx7
You would be surprised what people will do to try and not be accountable. I knw that another business would do everything to try and tune a car so they could make money. So Tsm not wanting to even mess with it raises some flags. Let me ask you this....why was it not tuned right the first time? Why were those afrs lean? Why did they let it leave like that?
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I asked that same question to Travis about well if the car is ok why the AFR's. His response was could be as simple as an o2 sensor, he said that JBA LT's are notorious for running lean until they have been corrected. either way he seem confident that the car was completely fine and that he would have it all corrected after he dyno tunes the car.
__________________
2014 5.0 Oxford White w/ Track Pack, 3.73's,
SR Lwr Ctrl Arms, Flowmaster Proseries AB,
Whiteline MT-82 bushing, JLT CAI, Bama Tune
1993 Cobra Black
Bbk shorty's, x-pipe, Flowmasters, bbk TB, bbk Cai,
UD pullies
(240rwhp/280rwtq)
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02-07-2014, 12:27 AM
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#3
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Senior Member
Join Date: Jun 2012
Location: Plano TX
Posts: 383
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re-rx7, IIRC the OP was using a SCT tune so it was not a custom tune. Was the AFR actually lean or was the tailpipe sniffer (which reads a little lean to begin with due to the distance away from the head) using a sensor that hadn't been calibrated for the fuel being used {14.08 instead of 14.64} or hadn't been changed recently since they degrade quickly when using mixed fuels?
Not saying TSM was wrong and GH is right.
What if GH is right and TSM is wrong? Then the red flag I see is that the OP ended up calling TSMs bluff on needing other services to fix his problem that was nonexistent by taking it elsewhere.
What if TSM is right and GH is wrong? Then the OP may be in trouble.
__________________
2010 GT500
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02-07-2014, 12:31 AM
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#4
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Banned
Join Date: Apr 2013
Location: Gainesville,Tx
Age: 39
Posts: 2,405
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Oh I see now. The thread has been confusing. First he had a custom tune then a canned. Lol idk what to believe! I don't think TS offered other services? I'm pretty sure the guy was using 93 and even if the tailpipe sniffer is further out 3 points is a lot
Last edited by re-rx7; 02-07-2014 at 12:34 AM.
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02-07-2014, 12:34 AM
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#5
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Senior Member
Join Date: Jan 2014
Location: TX
Posts: 285
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Originally Posted by re-rx7
Oh I see now. The thread has been confusing. First he ha a custom tune then a canned. Lol idk what to believe!
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i def never had a custom tune.
__________________
2014 5.0 Oxford White w/ Track Pack, 3.73's,
SR Lwr Ctrl Arms, Flowmaster Proseries AB,
Whiteline MT-82 bushing, JLT CAI, Bama Tune
1993 Cobra Black
Bbk shorty's, x-pipe, Flowmasters, bbk TB, bbk Cai,
UD pullies
(240rwhp/280rwtq)
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02-07-2014, 12:56 AM
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#6
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Senior Member
Join Date: May 2013
Posts: 275
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Yeah from everything I've read TSM are stand up guys- even giving someone their money back even though they were out time and labor.
I've also read some GREAT things about GearHeads and right now I'm between which one to use.
Regardless...it sounds like the problem could be- the guy was running an email tune with an o/r x pipe and LTs. I personally would never run on an email tune with that extensive of exhaust mods. I hope everything is ok.
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02-07-2014, 12:59 AM
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#7
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Senior Member
Join Date: Jan 2014
Location: TX
Posts: 285
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Thanks man, I hope to report some good news late tomorrow
__________________
2014 5.0 Oxford White w/ Track Pack, 3.73's,
SR Lwr Ctrl Arms, Flowmaster Proseries AB,
Whiteline MT-82 bushing, JLT CAI, Bama Tune
1993 Cobra Black
Bbk shorty's, x-pipe, Flowmasters, bbk TB, bbk Cai,
UD pullies
(240rwhp/280rwtq)
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02-07-2014, 01:02 AM
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#8
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Banned
Join Date: Apr 2013
Location: Gainesville,Tx
Age: 39
Posts: 2,405
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From what I've researched cat deletes a tune isn't needed. Now for the lt's I'm not sure.
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02-07-2014, 01:36 PM
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#9
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Senior Member
Join Date: Jan 2014
Location: TX
Posts: 285
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Just got a call from GH saying car did awesome and is ready to be picked up. Havent got any of the specks yet will let you know when i do.
__________________
2014 5.0 Oxford White w/ Track Pack, 3.73's,
SR Lwr Ctrl Arms, Flowmaster Proseries AB,
Whiteline MT-82 bushing, JLT CAI, Bama Tune
1993 Cobra Black
Bbk shorty's, x-pipe, Flowmasters, bbk TB, bbk Cai,
UD pullies
(240rwhp/280rwtq)
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02-07-2014, 02:00 PM
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#10
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Senior Member
Join Date: Jun 2012
Location: Plano TX
Posts: 383
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Thumbs up!
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2010 GT500
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02-07-2014, 03:26 PM
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#11
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Senior Member
Join Date: Jul 2012
Location: Roanoke, Texas
Age: 40
Posts: 818
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Cool! Very interested to hear how id did / is running.
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Airaid CAI | Borla S-Type Catback | Amsoil 10w30 and MTG Trans. Fluid
382hp 387ft/lb | 1/4: 12.9 @ 112mph
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02-07-2014, 05:43 PM
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#12
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Senior Member
Join Date: Jan 2014
Location: TX
Posts: 285
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Alright Fellas I just went by GH and talked with Travis...Car is running awesome and he said the LT's were throwing off the AFR but once he corrected the problem he said It dyno tuned perfectly. Its now running at 415 hp/402 Tq. I have the Dyno results scanned into my work computer but its saying file too big to upload so once I get back home to my Mac I can fix it and upload it. A big thanks to Travis and the GH's crew!!!
__________________
2014 5.0 Oxford White w/ Track Pack, 3.73's,
SR Lwr Ctrl Arms, Flowmaster Proseries AB,
Whiteline MT-82 bushing, JLT CAI, Bama Tune
1993 Cobra Black
Bbk shorty's, x-pipe, Flowmasters, bbk TB, bbk Cai,
UD pullies
(240rwhp/280rwtq)
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02-07-2014, 05:54 PM
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#13
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Senior Member
Join Date: Jun 2012
Posts: 5,594
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Originally Posted by Soulowd
Alright Fellas I just went by GH and talked with Travis...Car is running awesome and he said the LT's were throwing off the AFR but once he corrected the problem he said It dyno tuned perfectly. Its now running at 415 hp/402 Tq. I have the Dyno results scanned into my work computer but its saying file too big to upload so once I get back home to my Mac I can fix it and upload it. A big thanks to Travis and the GH's crew!!!
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That definitely sounds more legit! Congrats!
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02-07-2014, 05:50 PM
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#14
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Banned
Join Date: Apr 2013
Location: Gainesville,Tx
Age: 39
Posts: 2,405
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Now that sounds about right. Congrats on getting the power. How does it feel?
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02-07-2014, 06:01 PM
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#15
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Senior Member
Join Date: Jan 2014
Location: TX
Posts: 285
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Originally Posted by re-rx7
Now that sounds about right. Congrats on getting the power. How does it feel?
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Feels awesome! but im gonna need to invest in some tires cause I couldnt hook up in 1st and 2nd lol
__________________
2014 5.0 Oxford White w/ Track Pack, 3.73's,
SR Lwr Ctrl Arms, Flowmaster Proseries AB,
Whiteline MT-82 bushing, JLT CAI, Bama Tune
1993 Cobra Black
Bbk shorty's, x-pipe, Flowmasters, bbk TB, bbk Cai,
UD pullies
(240rwhp/280rwtq)
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