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07-27-2013, 04:06 PM
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#1
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Senior Member
Join Date: Oct 2012
Location: Fort Worth
Age: 54
Posts: 119
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Check engine light
Mine came on yesterday. Plugged the SCT in and code says Random misfire detected. anyone had this yet?
31,000 miles on the car, Is it time for a tune up? new plugs etc? I do not know a lot about engines, but can change plugs if thats all i need to do.
What else could it be? any input will be appreciated.
Thanks
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07-27-2013, 04:12 PM
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#2
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Senior Member
Join Date: Mar 2013
Age: 34
Posts: 1,047
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Originally Posted by Pat McCrotch
Mine came on yesterday. Plugged the SCT in and code says Random misfire detected. anyone had this yet?
31,000 miles on the car, Is it time for a tune up? new plugs etc? I do not know a lot about engines, but can change plugs if thats all i need to do.
What else could it be? any input will be appreciated.
Thanks
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Could be a lot of different issues. The cheapest would be to swap coils on the misfiring cylinder and see if the misfire moves. If it does move, replace it. I typically replace all of the coils and plugs for good measure. If you can and it's still under warranty, put it to stock and take it in.
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The Queen:
2013 Race Red Mustang GT 6MT: 20" AMR's, GT500 AB, JBA LT's and ORX, SCT SF3/X3, MGW Short Throw, Some Carbon Wrap, Spoiler Delete, Eibach Sportlines, Koni STR.T's, BMR LCA's, BMR Relo Brackets, BMR UCA, Freedom Racing PHB, Maximum Motorsports CC Plates, BMR Safety loop, DSS Aluminum DS
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07-27-2013, 04:34 PM
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#3
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Senior Member
Join Date: Oct 2012
Location: Fort Worth
Age: 54
Posts: 119
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with headers and catted X, cant really put it back to stock. and not sure what one is misfiring, it just said random misfire detected. Guess i will change all of them and go from there. Thanks
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07-27-2013, 04:43 PM
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#4
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Senior Member
Join Date: Mar 2013
Age: 34
Posts: 1,047
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Originally Posted by Pat McCrotch
with headers and catted X, cant really put it back to stock. and not sure what one is misfiring, it just said random misfire detected. Guess i will change all of them and go from there. Thanks
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I meant the tune. Idk how they'd feel about exhaust but some dealers are more lenient than others.
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The Queen:
2013 Race Red Mustang GT 6MT: 20" AMR's, GT500 AB, JBA LT's and ORX, SCT SF3/X3, MGW Short Throw, Some Carbon Wrap, Spoiler Delete, Eibach Sportlines, Koni STR.T's, BMR LCA's, BMR Relo Brackets, BMR UCA, Freedom Racing PHB, Maximum Motorsports CC Plates, BMR Safety loop, DSS Aluminum DS
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07-27-2013, 06:34 PM
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#5
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Senior Member
Join Date: Jun 2012
Location: Plano TX
Posts: 383
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Have you recently changed your clutch?
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2010 GT500
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07-27-2013, 07:49 PM
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#6
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Senior Member
Join Date: Oct 2012
Location: Fort Worth
Age: 54
Posts: 119
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Sometimes, I wish the car had a Clutch...
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07-27-2013, 08:12 PM
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#7
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Senior Member
Join Date: Jun 2012
Location: Plano TX
Posts: 383
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Have you changed the converter recently?
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2010 GT500
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07-27-2013, 08:19 PM
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#8
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Banned
Join Date: Apr 2013
Location: Gainesville,Tx
Age: 39
Posts: 2,405
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Weird. I went to downshift mine today from 3rd to 2nd and my car hiccuped and flashed the check engine light just for a sec. Back to normal after that.
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07-27-2013, 08:31 PM
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#9
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Senior Member
Join Date: Oct 2012
Location: Fort Worth
Age: 54
Posts: 119
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Originally Posted by Yagermeister
Have you changed the converter recently?
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Nope... Happened 1st a few days ago, I changed the tune that I have been running for over a year "93S" to the 93R. I had been so happy with the 93S I forgot about the 93R, so I tried it, code came in after 10 min of driving. Put the 93S back on, code went away, then 2 days later came back yesterday.
Last night, I loaded a different tune from different company, drove to and from work today with no issues yet, but is still idling a little rough.
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07-27-2013, 08:55 PM
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#10
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Senior Member
Join Date: Jun 2012
Location: Plano TX
Posts: 383
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Clear the KAM and do an idle relearn and you'll probably be good
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2010 GT500
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07-28-2013, 08:15 PM
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#11
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Senior Member
Join Date: Oct 2012
Location: Fort Worth
Age: 54
Posts: 119
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I will try that when I get back in town.. One thing I did notice before I left, It looked like one of the hoses going to the Moroso air/oil separator was collapsed in one spot.
I am definitely going to get better hose to change that out, but could this be what caused the random misfire code?
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07-28-2013, 08:44 PM
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#12
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Senior Member
Join Date: Jun 2012
Location: Plano TX
Posts: 383
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Not sure about that but IF you had changed your clutch or converter you should do a misfire profile correction procedure at the dealer.
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2010 GT500
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07-29-2013, 09:15 PM
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#13
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Senior Member
Join Date: Jun 2012
Location: Plano TX
Posts: 383
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Loose crank position sensor maybe?
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2010 GT500
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07-29-2013, 11:04 PM
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#14
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Senior Member
Join Date: Jul 2013
Age: 46
Posts: 180
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Originally Posted by Yagermeister
Loose crank position sensor maybe?
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This...common issue on the coyotes. You could also pull a plug to see if its fouled. I know mine were fouled out bad from the Trackey programming running lean up top.
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Chad
2012 PW Boss 302 #2550 - Current
2003 DSG Terminator #1410 - SOLD
2000 Black Lightning #4278 - SOLD
2007 RFP Mustang GT (Cammed/Procharged) - DEAD
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07-30-2013, 09:20 AM
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#15
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Senior Member
Join Date: Jun 2012
Posts: 697
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Mine got a steady Check Engine Light two days after the engine was replaced. It came back with random misfire codes for various cylinders. The dealer tech had to do a 'crankshaft position relearn' process and that cured it.
PS - I don't like your 'idling rough' comment because that was the first symptom of my piston letting go. After about five miles of rough idling, the CEL came on steady, then the next morning it began flashing. The piston on cylinder 8 had cracked the top ring land. Hope yours is something else.
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"If this was like, a thousand years ago, I'd be a Picasso. I'd be one of those dudes that cut his damned ear off."
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